![]() |
#1 |
TST Ruined My Life!
|
Trouble boosting
__________________
III To view links or images in signatures your post count must be 10 or greater. You currently have 0 signatures. |
![]() |
![]() |
![]() |
#2 |
Tri-State Post Whore
|
throw another bov on there, if it goes back to the way it was then that was the problem...if not, it would inspect all hose couplings again......or if you wanted to get crazy you could ditch the whole stock thing, and go vf34, Access port and a FMIC, and that would solve just about any problem
__________________
Bill If you guys see a possum...try to kill it, it's not a pet! |
![]() |
![]() |
![]() |
#4 |
TST Ruined My Life!
|
I just needed to turn the boost controller a little more with the stocker on there. Actually, the stock bypass holds alot better then my greddy did. I drop less then one PSI now at high RPM.. WOOT!!
__________________
III To view links or images in signatures your post count must be 10 or greater. You currently have 0 signatures. |
![]() |
![]() |
![]() |
Bookmarks |
|
|
![]() |
||||
Thread | Thread Starter | Forum | Replies | Last Post |
Sputtering, Spooling but not boosting... | 609 GST | General Car Related Chat | 5 | 02-15-2010 03:24 AM |
boosting a 420a | cxrock16 | General Car Related Chat | 26 | 06-02-2008 07:22 PM |
KA-T boosting problem | s14drftstn | Nissan / Infiniti Talk | 15 | 03-24-2008 04:33 PM |
Boosting | TunedIS300 | Pennsylvania | 7 | 03-12-2008 11:58 PM |
04 stillen supercharged z not boosting! help | Im2Slow | Engine Performance | 33 | 08-24-2007 06:20 PM |